| What went wrong on LR2007? | |
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+84x4Bun Sparky CarpeDiem TonySLROC Badger VentureOverland theshortwayround andybloke 12 posters |
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andybloke Admin
Number of posts : 1090 Age : 47 Localisation : West Yorkshire Registration date : 2007-06-03
| Subject: What went wrong on LR2007? Tue Sep 25, 2007 8:49 am | |
| There were various technical problems on LR2007, some confirmed, some just hearsay....
What went wrong, if anything, on your vehicle?
To start off: Lara Landy (the Tombraider D90 Td5), Team Remember Chernobyl Hose between the turbo and intercooler venting air under boost - twelve turns (!) of the jubilee clip screw before the offroad course cured that. Immobiliser randomly kicking in/ECU locking out (usually when the engine was off, but also on motorways, mountain roads, etc). Tail light went, but blew the fuse on the reverse/brake lights. GPS-to-internet system broke down on the ferry home! | |
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theshortwayround
Number of posts : 444 Localisation : Berkshire Registration date : 2007-04-26
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 8:58 am | |
| 300 Tdi Disco - theshortwayround,
Overheat whilst in traffic, blew plastic crap (sorry - cap) on top of thermostat housing as fans failed to start.
Turbo pipe blew off - quickly put back on.
Still overheating even though cap repaired, then replaced with brass one, and stage one fan hard wired on.
Thermostate reloacted to boot, stage 2 of fan hard wired in, no further problems.
Would seam Thermostat at fault, originally felt that fan temp sender had failed, and therfore heat casued by no engine fans on. felt this then casued thermostat to fail in the closed position.
Thoughts now, are that thermostat had failed, this casued bad circulation of water throgh rad, therfore water at fan temp sender not hot enough to engage either stage of fan.
New Thermostat and fan temp sender being fitted for good measure!
Now home, Alarm going off all through the night to the delight of my good neighbours. unsire as to reason, no apparent faults, and is only going off at night. At fault? maybe some scroats planning on bad ideas with my Disco. either that, or sensor fault. In to Main dealer (Ouch, but what can you do!) in the week to get seen too.
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VentureOverland
Number of posts : 606 Localisation : Sydney, Australia Registration date : 2007-02-19
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 9:26 am | |
| Team VentureOverland 1: - Blew an auxillary fuse when I trapped the 12V flourescent light cable in the door latch - arse!
Team VentureOverland 2: - Had a habbit of dropping all its oil out of the T/Box. When VO1 was following, when we didnt need the wipers any more it was time to stop and refill the lead T/Box!!!! - A little bit of brake fade on the way down from Val d'Isere. A cup of coffee soon fixed that... or perhaps it was the time taken to make the coffee!!??
No major shakes in this camp then... | |
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Badger
Number of posts : 145 Age : 54 Localisation : Surrey Registration date : 2007-01-29
| Subject: My Truck - Range Rover P38A Tue Sep 25, 2007 9:32 am | |
| Very poor mileage from a tank of LPG - about 280 miles average on a 80l tank fill.
No Low range gears - suspect this is the selector motor - i hope so as i do not fancy having to fork out for a complete transfer box. this caused me to use the brakes all the way into val d'isere so they got hot and stinky and a "bit" vague
Engine a little hicoughy at 2.5 to 3k revs - going to the engine man to have a look. this was both on petrol and LPG.
used about 1 litre of oil.
interior light doesn't work - the individual map lights do but not the main centre one.
Off side (UK) tail light dim.
I think that is about it.
Cheers | |
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TonySLROC
Number of posts : 115 Localisation : Suffolk Registration date : 2007-04-20
| Subject: Problems Tue Sep 25, 2007 10:14 am | |
| Hi guys glad to see you are all back safely. I am well chuffed with the defender not a single problem!!! Regards Tony | |
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CarpeDiem
Number of posts : 549 Registration date : 2007-03-27
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 11:42 am | |
| Got hot uphills, and on long motorway journeys. Just had to lift off a bit.
Apart from that, just a fuse, for the 12v 4-way adaptor.
Back to Keith Gotts for a check over, service, check box as it jumps out of 2nd/sometimes 3rd on over-run (it did before), and replace exhaust system. (for £50 it's not worth welding it)
Cheers, Mark | |
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Sparky
Number of posts : 32 Registration date : 2007-02-16
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 12:24 pm | |
| Dumped a bit of oil from somewhere, lots of it on the bottom of rear axle but not much indication from whence it came. Seems to have an injector problem at a certain rev range, just stutters a bit every now and then.
BUT Mandy covered the fridge air circulation vents over drying a towel !!!!!!!
It overheated switched off and all the beer got warm.... disaster | |
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CarpeDiem
Number of posts : 549 Registration date : 2007-03-27
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 1:21 pm | |
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4x4Bun
Number of posts : 40 Age : 47 Localisation : Hampshire Registration date : 2007-08-07
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 1:31 pm | |
| Team Thames Valley 4x4 - blew a fuse on the CD player - cause Lucky Trucker playing 'Rule Britannia' way too loud on the flag waving convoy through Calais on Day1 We then blew another fuse when the inverter decided it really didn't like my laptop being plugged in Apart from that, no problems to report.....result Bun :flower: | |
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Tom Mc Organiser
Number of posts : 3925 Registration date : 2007-01-29
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 1:37 pm | |
| Bad news about the warm beer chaps - what a bummer!Slight loss of power in the mountains due to the ECU panicing over the thin air. Bloody electronics, didn't have that trouble with my 2-door Rangies! The miniscule blow on the Rangie's downpipe got a bit worse. Passenger's door handle broke (cast alloy). Arriving back at Calais I drove straight on the ramp at Jean-Luc Guyot's garage. He dropped everything and repaired it there and then. After he plied Badger, Dr Evil, Rafe and myself with four large glasses of Ricard. Badger/Dr Evil said thanks but no thanks a departed quick sharp, leaving myself and Rafe to face the aniseed lake. With Rafe volunteering to drive, having downed one I was then presented with Badger's glassful. Half-cut at 2pm with loads of work to do back at Cafe de Paris getting the prize-giving sorted. HELP!!!!! Jean Luc even brought a replacement secondhand door handle with him to the dinner that evening - what a good bloke! Can't think of anything at all mechanically, unlike some the £800 Rangie didn't skip a beat. | |
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Mel_f
Number of posts : 46 Localisation : West Sussex Registration date : 2007-09-02
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Lu and Tweedie
Number of posts : 343 Localisation : Macclesfield, Cheshire Registration date : 2007-05-14
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 2:42 pm | |
| Team T'n'T - 200 Tdi Disco. Clutch slave cylinder died in its sleep! It was fine coming down the mountains, but did not want to leave the campsite in Andorra! Fortunately we had taken a spare with us and had lots of support - cheers Fred and the Pukka Posse! Lots of fluid later and we were off again! Oh... and we popped several fuses in the cigarette lighter playing with flashing beacons and..... the fluffy dice fell off during the offroad course! Not too bad for 2900 miles door to door in 9 days (nearly 1/3 of an average person's yearly mileage!) Lu and T :bom: | |
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Guest Guest
| Subject: Re: What went wrong on LR2007? Tue Sep 25, 2007 3:04 pm | |
| 200 tdi 90 i was impressed with it during the trip only the transfer box ran out of oil in the alps, and the welds that we did on the back door broke due to the good vibrations caused by speed. got it home and there has been oil spraying out of the oil filler cap ontop of engine, the fuel intake pipe has a hole in it and appears to suck air in to engine when starting up rear shockers may have gone will get us to abingdon im sure now half wired up andy blokes switches thankyou very much i owe you beer :!: :!: :!: cheers kieran |
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Dorset4x4
Number of posts : 38 Localisation : Blandford Forum Dorset Registration date : 2007-04-23
| Subject: Re: What went wrong on LR2007? Wed Sep 26, 2007 2:29 pm | |
| Electrical connection came off the starter twice. Not bad for a £600.00 22 year old 110 ok ok I konw I spent about £500 on the 200 TDI and pipe kit. Bet it would have been more comfortable in the 300 TDI Disco, gone but not forgoten. Series has new engine and is running again, might pop it in a pond again this weekend | |
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VentureOverland
Number of posts : 606 Localisation : Sydney, Australia Registration date : 2007-02-19
| Subject: Re: What went wrong on LR2007? Thu Sep 27, 2007 3:05 am | |
| - kieran wrote:
- 200 tdi 90
got it home and there has been oil spraying out of the oil filler cap ontop of engine
Kieren, This perhaps isnt good news... Im assuming you had the oil filler cap on and its a decent fit. If the cap was missing or a very crap fit ignore below... If so then the rocker casing is pressurizing. That means that the sump is running at pressure and that pressure is being released by the sump breather which feeds back into the rocker cover. There are a few reasons that the sump will be pressurizing, but lets hope you just need a quick head gasket change. Normally on a 200tdi the H/G lets go between the back two pots, but chances are you have a leak between (im guessing now) one of those two back cylinders and one of the oil capillary tubes in the block. That being the case, a % of your compression isbeing forced down the capillary and into the sump... As another check, with the engine running (tick over), remove the dipstick and listen carefully. I reckon you'll here a "chuff-chuff" sort of noise coming from the dipstick, indicating a pressurised sump. Good news is head gaskets are easy to change and / or I could be completely wrong!! | |
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theshortwayround
Number of posts : 444 Localisation : Berkshire Registration date : 2007-04-26
| Subject: Re: What went wrong on LR2007? Fri Sep 28, 2007 8:03 am | |
| sounds like a get together around keirans motor tomorrow then!!
:arrow: | |
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Guest Guest
| Subject: Re: What went wrong on LR2007? Fri Sep 28, 2007 11:47 am | |
| hello, cheers for the advice jon, i have just braved the cold and the rain and gone and tryed to listen to the dipstick hole but i have just driven to sheffield and back (54 miles) and i was abit def god knows how i made it through landy rally but there was a chuff chuff noise but i couldnt work out whether that was coming from the engine noise so ill try again before setting off tomorrow now for the embaressing storey : today i was checking all of the oil levels on the landy, i checked the gear box level and splat 2 litres of oil came heading my way from our emergiency fill up in switserland without properly reading the haynes guide book of vagueness that doesnt tell you much ( we put the oil in the wrong hole and ran 150 miles with no oil in the transer box oooops but hey look on the brigh side the gears seem to move so much more smoothly now any one taking a marquee to the show may need it with this rain ! cheers kieran |
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Guest Guest
| Subject: Re: What went wrong on LR2007? Fri Sep 28, 2007 11:50 am | |
| i hope its not a head gasket my brother has just payed 850 squids to have his frontera fixed after his head gasket blow massivly |
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4x4Bun
Number of posts : 40 Age : 47 Localisation : Hampshire Registration date : 2007-08-07
| Subject: Re: What went wrong on LR2007? Fri Sep 28, 2007 2:45 pm | |
| 4x4Bun was not completly right about Team TV4x4. We left Reading with a t-box oil leak, when it stopped leaking at Andora it was time to top it up again. Oil leak restored, all happy | |
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VentureOverland
Number of posts : 606 Localisation : Sydney, Australia Registration date : 2007-02-19
| Subject: Re: What went wrong on LR2007? Mon Oct 01, 2007 1:16 am | |
| - kieran wrote:
- i hope its not a head gasket my brother has just payed 850 squids to have his frontera fixed after his head gasket blow massivly
Kieren, If it does transpire to be the head gasket - dont pay £850 to have it done... Study the Haynes manual, spend £30 on a gasket set and tackle it yourself. It really is an easy job, if you take your time and plan what you are doing. The two most important things are to a) get the head gasket the right way up and round and b) torque the head bolts down in the right order and to the right torque. All of which is detailed well in the Haynes Manual. All that said though Im not entirely convinced your oil problem is caused by a failed / failing H/G. | |
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